HomeMy WebLinkAboutPost inspection report, US-FL-5014_FPR-006-FM-Studio VB TIA Maintenance COP
POST CONSTRUCTION INSPECTION REPORT
US-FL-5014 – FPR-006-FM-Studio, 360-ft Guyed Tower
ETS#: 200688.CO
December 21st, 2020
Page 1 of 22
3227 Wellington Court, Raleigh, NC 27615 o) 919.782.2710
www.engineeredtowersolutions.com
POST CONSTRUCTION CLOSE OUT REPORT
SITE NAME: FPR-006-FM-STUDIO (US-FL-5014)
Performed By:
Prepared for:
POST CONSTRUCTION INSPECTION REPORT
US-FL-5014 – FPR-006-FM-Studio, 360-ft Guyed Tower
ETS#: 200688.CO
December 21st, 2020
Page 2 of 22
3227 Wellington Court, Raleigh, NC 27615 o) 919.782.2710
www.engineeredtowersolutions.com
1.0 ASSIGNMENT
Subject – Post construction report of an existing guyed tower
Location – 6690 North US #1, Fort Pierce, FL 34945
Structure – 360-ft Guyed Tower
Purpose – Resolve select issues noted in the TIA report dated April 27, 2020.
2.0 SCOPE OF SERVICES
1. REMOVE VEGETATION AND DEBRIS IN TOWER COMPOUND. REGRADE COMPOUND SUCH
THAT TOWER BASE FOUNDATION IS FLUSH WITH FINISHED GRADE. INSTALL GEOFABRIC
MAT AND GRAVEL TO A DEPTH OF 4".
2. CLEAN AREAS OF CORROSION ON TOWER AND APPLY TWO COATS OF ZINC RICH COLD
GALVANIZING COMPOUND.
3. CAD WELD GROUND WIRES TO TOWER LEGS.
4. REPLACE DAMAGED HORIZONTAL MEMBER AND ALL CONNECTION HARDWARE ON CA
FACE. 140’
5. CLEAN AREA OF CORROSION ON A-LEG FLANGE AND APPLY TWO COATS OF ZINC RICH
COLD GALVANIZING COMPOUND. IF MATERIAL LOSS IS OBSERVED PROVIDE
DOCUMENTATION TO EOR FOR DETERMINATION OF ANY FURTHER ACTION. 140’
6. CLEAN AREAS OF CORROSION ON TOWER BASE PLATE AND APPLY TWO COATS OF ZINC
RICH COLD GALVANIZING COMPOUND. IF MATERIAL LOSS IS OBSERVED PROVIDE
DOCUMENTATION TO EOR FOR DETERMINATION OF ANY FURTHER ACTION.
7. INSTALL MISSING FLANGE BOLT ON A-LEG (A325 3/4"Øx2-1/2" W/ NUT/LOCK WASHER). 340’
8. CLEAN AREA OF CORROSION ON B-LEG AND APPLY TWO COATS OF ZINC RICH COLD
GALVANIZING COMPOUND. IF MATERIAL LOSS IS OBSERVED PROVIDE DOCUMENTATION
TO EOR FOR DETERMINATION OF ANY FURTHER ACTION. 360’
9. REPLACE GUY WIRES AND ALL GUY CONNECTION HARDWARE. 280’
10. INSTALL LIGHTNING ROD TO EXTEND 4' ABOVE HIGHEST APPURTENANCE. 360’
11. EXCAVATE GUY ANCHOR RODS TO FOUNDATION BLOCK. CLEAN AREAS OF CORROSION
AND COAT WITH DENSO PROTAL 7125. IF MATERIAL LOSS IS OBSERVED PROVIDE
DOCUMENTATION TO EOR FOR DETERMINATION OF ANY FURTHER ACTION.
12. CLEAN AREAS OF CORROSION ON GUY HARDWARE AND APPLY TWO COATS OF ZINC RICH
COLD GALVANIZING COMPOUND. 0’, 80’, 160’, 220’, 340’
13. REPLACE CORRODED COTTER PINS. 0’
14. INSTALL MOUSING ON SCREW PIN SHACKLES. 0’, 80’, 160’, 220’, 340’
15. INSTALL GUY WIRE END SERVINGS. 0’, 80’, 160’, 220’, 340’
16. REPLACE TURNBUCKLE SAFETY CABLES WITH 3/8" GALVANIZED WIRE ROPE, (2) CROSBY
CLAMPS EACH. INSTALL IN FIGURE 8 CONFIGURATION.
17. INSTALL GUY ANCHOR COMPOUNDS AT ALL ANCHORS.
18. REMOVE CUT COAX ON B-LEG. 0’ – 59’
19. INSTALL SAFETY CLIMB SYSTEM ON TOWER. 0’ – 360’
20. ADJUST GUY TENSIONS AND TOWER TWIST & PLUMB.
POST CONSTRUCTION INSPECTION REPORT
US-FL-5014 – FPR-006-FM-Studio, 360-ft Guyed Tower
ETS#: 200688.CO
December 21st, 2020
Page 3 of 22
3227 Wellington Court, Raleigh, NC 27615 o) 919.782.2710
www.engineeredtowersolutions.com
3.0 PARTICIPATING PERSONNEL
Carrier Representatives: Kyle Lee Sing
Senior Operations Support Manager
Vertical Bridge Holding, LLC
750 Park of Commerce Drive
Suite 200
Boca Raton, FL 33487
561.406.4022
kleesing@verticalbridge.com
ETS Representative: George Finley, PMP
Engineered Tower Solutions, PLLC
3227 Wellington Court
Raleigh, NC 27615
(704) 968-3729
George.Finley@ets-pllc.com
4.0 BACKGROUND INFORMATION
Vertical Bridge requested that ETS complete maintenance repairs on the subject structure. The
construction was to repair select deficiencies noted in the following document:
x 5/4/20 Engineered Tower Solutions TIA Maintenance Drawings 200688.14 Rev# 0
5.0 RESULTS
1. All work was completed per provided documentation
POST CONSTRUCTION INSPECTION REPORT
US-FL-5014 – FPR-006-FM-Studio, 360-ft Guyed Tower
ETS#: 200688.CO
December 21st, 2020
Page 4 of 22
3227 Wellington Court, Raleigh, NC 27615 o) 919.782.2710
www.engineeredtowersolutions.com
EXECUTIVE SUMMARY
Photograph Observations and Recommendations
Site Sign
Item 1
Observation:
REMOVE VEGETATION AND DEBRIS IN TOWER
COMPOUND. REGRADE COMPOUND SUCH THAT
TOWER BASE FOUNDATION IS FLUSH WITH
FINISHED GRADE. INSTALL GEOFABRIC MAT
AND GRAVEL TO A DEPTH OF 4".
Recommendations:
None.
POST CONSTRUCTION INSPECTION REPORT
US-FL-5014 – FPR-006-FM-Studio, 360-ft Guyed Tower
ETS#: 200688.CO
December 21st, 2020
Page 5 of 22
3227 Wellington Court, Raleigh, NC 27615 o) 919.782.2710
www.engineeredtowersolutions.com
EXECUTIVE SUMMARY
Photograph Observations and Recommendations
Item 2
Observation:
CLEAN AREAS OF CORROSION ON TOWER AND
APPLY TWO COATS OF ZINC RICH COLD
GALVANIZING COMPOUND.
Recommendations:
None.
POST CONSTRUCTION INSPECTION REPORT
US-FL-5014 – FPR-006-FM-Studio, 360-ft Guyed Tower
ETS#: 200688.CO
December 21st, 2020
Page 6 of 22
3227 Wellington Court, Raleigh, NC 27615 o) 919.782.2710
www.engineeredtowersolutions.com
EXECUTIVE SUMMARY
Photograph Observations and Recommendations
Item 3
Observation:
CAD WELD GROUND WIRES TO TOWER LEGS.
Recommendations:
None.
POST CONSTRUCTION INSPECTION REPORT
US-FL-5014 – FPR-006-FM-Studio, 360-ft Guyed Tower
ETS#: 200688.CO
December 21st, 2020
Page 7 of 22
3227 Wellington Court, Raleigh, NC 27615 o) 919.782.2710
www.engineeredtowersolutions.com
EXECUTIVE SUMMARY
Photograph Observations and Recommendations
Item 4
Observation:
REPLACE DAMAGED HORIZONTAL MEMBER
AND ALL CONNECTION HARDWARE ON CA
FACE. 140’
Recommendations:
None.
POST CONSTRUCTION INSPECTION REPORT
US-FL-5014 – FPR-006-FM-Studio, 360-ft Guyed Tower
ETS#: 200688.CO
December 21st, 2020
Page 8 of 22
3227 Wellington Court, Raleigh, NC 27615 o) 919.782.2710
www.engineeredtowersolutions.com
EXECUTIVE SUMMARY
Photograph Observations and Recommendations
Item 5
Observation:
CLEAN AREA OF CORROSION ON A-LEG FLANGE
AND APPLY TWO COATS OF ZINC RICH COLD
GALVANIZING COMPOUND. IF MATERIAL LOSS
IS OBSERVED PROVIDE DOCUMENTATION TO
EOR FOR DETERMINATION OF ANY FURTHER
ACTION. 140’
Recommendations:
None.
POST CONSTRUCTION INSPECTION REPORT
US-FL-5014 – FPR-006-FM-Studio, 360-ft Guyed Tower
ETS#: 200688.CO
December 21st, 2020
Page 9 of 22
3227 Wellington Court, Raleigh, NC 27615 o) 919.782.2710
www.engineeredtowersolutions.com
EXECUTIVE SUMMARY
Photograph Observations and Recommendations
Item 6
Observation:
CLEAN AREAS OF CORROSION ON TOWER BASE
PLATE AND APPLY TWO COATS OF ZINC RICH
COLD GALVANIZING COMPOUND. IF MATERIAL
LOSS IS OBSERVED PROVIDE DOCUMENTATION
TO EOR FOR DETERMINATION OF ANY FURTHER
ACTION.
Recommendations:
None.
POST CONSTRUCTION INSPECTION REPORT
US-FL-5014 – FPR-006-FM-Studio, 360-ft Guyed Tower
ETS#: 200688.CO
December 21st, 2020
Page 10 of 22
3227 Wellington Court, Raleigh, NC 27615 o) 919.782.2710
www.engineeredtowersolutions.com
EXECUTIVE SUMMARY
Photograph Observations and Recommendations
Item 7
Observation:
INSTALL MISSING FLANGE BOLT ON A-LEG (A325
3/4"Øx2-1/2" W/ NUT/LOCK WASHER). 340’
Recommendations:
None.
Photograph Observations and Recommendations
Item 8
Observation:
CLEAN AREA OF CORROSION ON B-LEG AND
APPLY TWO COATS OF ZINC RICH COLD
GALVANIZING COMPOUND. IF MATERIAL LOSS
IS OBSERVED PROVIDE DOCUMENTATION TO
EOR FOR DETERMINATION OF ANY FURTHER
ACTION. 360’
Recommendations:
None.
POST CONSTRUCTION INSPECTION REPORT
US-FL-5014 – FPR-006-FM-Studio, 360-ft Guyed Tower
ETS#: 200688.CO
December 21st, 2020
Page 11 of 22
3227 Wellington Court, Raleigh, NC 27615 o) 919.782.2710
www.engineeredtowersolutions.com
EXECUTIVE SUMMARY
Photograph Observations and Recommendations
Item 9
Observation:
REPLACE GUY WIRES AND ALL GUY
CONNECTION HARDWARE. 280’
Recommendations:
None.
POST CONSTRUCTION INSPECTION REPORT
US-FL-5014 – FPR-006-FM-Studio, 360-ft Guyed Tower
ETS#: 200688.CO
December 21st, 2020
Page 12 of 22
3227 Wellington Court, Raleigh, NC 27615 o) 919.782.2710
www.engineeredtowersolutions.com
EXECUTIVE SUMMARY
Photograph Observations and Recommendations
Item 10
Observation:
INSTALL LIGHTNING ROD TO EXTEND 4' ABOVE
HIGHEST APPURTENANCE. 360’
Recommendations:
None.
POST CONSTRUCTION INSPECTION REPORT
US-FL-5014 – FPR-006-FM-Studio, 360-ft Guyed Tower
ETS#: 200688.CO
December 21st, 2020
Page 13 of 22
3227 Wellington Court, Raleigh, NC 27615 o) 919.782.2710
www.engineeredtowersolutions.com
EXECUTIVE SUMMARY
Photograph Observations and Recommendations
Item 11
Observation:
EXCAVATE GUY ANCHOR RODS TO
FOUNDATION BLOCK. CLEAN AREAS OF
CORROSION AND COAT WITH DENSO PROTAL
7125. IF MATERIAL LOSS IS OBSERVED PROVIDE
DOCUMENTATION TO EOR FOR DETERMINATION
OF ANY FURTHER ACTION.
Recommendations:
None.
POST CONSTRUCTION INSPECTION REPORT
US-FL-5014 – FPR-006-FM-Studio, 360-ft Guyed Tower
ETS#: 200688.CO
December 21st, 2020
Page 14 of 22
3227 Wellington Court, Raleigh, NC 27615 o) 919.782.2710
www.engineeredtowersolutions.com
EXECUTIVE SUMMARY
Photograph Observations and Recommendations
Item 12
Observation:
CLEAN AREAS OF CORROSION ON GUY
HARDWARE AND APPLY TWO COATS OF ZINC
RICH COLD GALVANIZING COMPOUND. 0’, 80’,
160’, 220’, 340’
Recommendations:
None.
POST CONSTRUCTION INSPECTION REPORT
US-FL-5014 – FPR-006-FM-Studio, 360-ft Guyed Tower
ETS#: 200688.CO
December 21st, 2020
Page 15 of 22
3227 Wellington Court, Raleigh, NC 27615 o) 919.782.2710
www.engineeredtowersolutions.com
EXECUTIVE SUMMARY
Photograph Observations and Recommendations
Item 13
Observation:
REPLACE CORRODED COTTER PINS. 0’
Recommendations:
None.
POST CONSTRUCTION INSPECTION REPORT
US-FL-5014 – FPR-006-FM-Studio, 360-ft Guyed Tower
ETS#: 200688.CO
December 21st, 2020
Page 16 of 22
3227 Wellington Court, Raleigh, NC 27615 o) 919.782.2710
www.engineeredtowersolutions.com
EXECUTIVE SUMMARY
Photograph Observations and Recommendations
Item 14
Observation:
INSTALL MOUSING ON SCREW PIN SHACKLES. 0’,
80’, 160’, 220’, 340’
Recommendations:
None.
POST CONSTRUCTION INSPECTION REPORT
US-FL-5014 – FPR-006-FM-Studio, 360-ft Guyed Tower
ETS#: 200688.CO
December 21st, 2020
Page 17 of 22
3227 Wellington Court, Raleigh, NC 27615 o) 919.782.2710
www.engineeredtowersolutions.com
EXECUTIVE SUMMARY
Photograph Observations and Recommendations
Item 15
Observation:
INSTALL GUY WIRE END SERVINGS. 0’, 80’, 160’,
220’, 340’
Recommendations:
None.
POST CONSTRUCTION INSPECTION REPORT
US-FL-5014 – FPR-006-FM-Studio, 360-ft Guyed Tower
ETS#: 200688.CO
December 21st, 2020
Page 18 of 22
3227 Wellington Court, Raleigh, NC 27615 o) 919.782.2710
www.engineeredtowersolutions.com
EXECUTIVE SUMMARY
Photograph Observations and Recommendations
Item 16
Observation:
REPLACE TURNBUCKLE SAFETY CABLES WITH
3/8" GALVANIZED WIRE ROPE, (2) CROSBY
CLAMPS EACH. INSTALL IN FIGURE 8
CONFIGURATION.
Recommendations:
None.
POST CONSTRUCTION INSPECTION REPORT
US-FL-5014 – FPR-006-FM-Studio, 360-ft Guyed Tower
ETS#: 200688.CO
December 21st, 2020
Page 19 of 22
3227 Wellington Court, Raleigh, NC 27615 o) 919.782.2710
www.engineeredtowersolutions.com
EXECUTIVE SUMMARY
Photograph Observations and Recommendations
Item 17
Observation:
INSTALL GUY ANCHOR COMPOUNDS AT ALL
ANCHORS.
Recommendations:
None.
POST CONSTRUCTION INSPECTION REPORT
US-FL-5014 – FPR-006-FM-Studio, 360-ft Guyed Tower
ETS#: 200688.CO
December 21st, 2020
Page 20 of 22
3227 Wellington Court, Raleigh, NC 27615 o) 919.782.2710
www.engineeredtowersolutions.com
EXECUTIVE SUMMARY
Photograph Observations and Recommendations
Item 18
Observation:
REMOVE CUT COAX ON B-LEG. 0’ – 59’
Recommendations:
None.
POST CONSTRUCTION INSPECTION REPORT
US-FL-5014 – FPR-006-FM-Studio, 360-ft Guyed Tower
ETS#: 200688.CO
December 21st, 2020
Page 21 of 22
3227 Wellington Court, Raleigh, NC 27615 o) 919.782.2710
www.engineeredtowersolutions.com
EXECUTIVE SUMMARY
Photograph Observations and Recommendations
Item 19
Observation:
INSTALL SAFETY CLIMB SYSTEM ON TOWER. 0’ –
360’
Recommendations:
None.
POST CONSTRUCTION INSPECTION REPORT
US-FL-5014 – FPR-006-FM-Studio, 360-ft Guyed Tower
ETS#: 200688.CO
December 21st, 2020
Page 22 of 22
3227 Wellington Court, Raleigh, NC 27615 o) 919.782.2710
www.engineeredtowersolutions.com
EXECUTIVE SUMMARY
Photograph Observations and Recommendations
See Attached Reports
Item 20
Observation:
ADJUST GUY TENSIONS AND TOWER TWIST &
PLUMB.
Recommendations:
None.
Plumb&TensionReports
6LWH
6LWH1DPH
&RQWUDFWRU1DPH
&RPSOHWHG%\
'DWH
7HPSHUDWXUH)
:LQG6SHHG03+
:LQG'LUHFWLRQ 66:
(Northernmost (A) Anchor)
6L]H 3KRWR
*3
/HIW 3KRWR5LJKW 3KRWR*3/HIW 5LJKW
*X\3XOO2II (+6 *5((1
*X\3XOO2II (+6 *5((1
*X\3XOO2II (+6 %/8(
*X\3XOO2II (+6 %/$&.
*X\3XOO2II (+6 25$1*(
(B Anchor)
6L]H 3KRWR
*3
/HIW 3KRWR5LJKW 3KRWR*3/HIW 5LJKW
*X\3XOO2II (+6 *5((1
*X\3XOO2II (+6 *5((1
*X\3XOO2II (+6 %/8(
*X\3XOO2II (+6 %/$&.
*X\3XOO2II (+6 25$1*(
&DEOH6L]H
PHDVXUHPHQW
6HH1RWHDERYH
3DLQW
&RORURQ
'HDG(QG
*ULS,I
YLVLEOH
0HDVXUHG7HQVLRQ/EV
8VH*3/HIWFROXPQIRU
*X\3XOO2II
6HH1RWHDERYH
'HVLJQ
,QLWLDO
7HQVLRQ
RI%6
&DOFXODWHG7HQVLRQ
RI'HVLJQ
'HVLJQ
,QLWLDO
7HQVLRQ
RI%6
&DOFXODWHG7HQVLRQ
RI'HVLJQ
*X\
/HYHO (OHY)W
'LVW7R
$QFKRU
)W
*X\
$WWDFKPHQW
7\SH
&DEOH
7\SH
&RPPHQWV
7HPS
)
86)/
)35)06WXGLR
:LOOLDP6KHSSDUG
&RPPHQWV
32677(16,21,1**8<7(16,210($685(0(176
*Note - Cable sizes must be measured with Guy Cable Measuring Tool.
Photos of size and tension measurements are required. If all cable sizes
at one elevation are the same for all legs, photos of size measurements
of only one leg are required.
*X\
/HYHO (OHY)W
'LVW7R
$QFKRU
)W
*X\
$WWDFKPHQW
7\SH
&DEOH
7\SH
&DEOH6L]H
PHDVXUHPHQW
*See Note above
3DLQW
&RORURQ
'HDG(QG
*ULS,I
YLVLEOH
0HDVXUHG7HQVLRQ/EV8VH
*3/HIWFROXPQIRU*X\3XOO
2II*See Note above7HPS
)
(C Anchor)
6L]H 3KRWR
*3
/HIW 3KRWR5LJKW 3KRWR*3/HIW 5LJKW
*X\3XOO2II (+6 *5((1
*X\3XOO2II (+6 *5((1
*X\3XOO2II (+6 %/8(
*X\3XOO2II (+6 %/$&.
*X\3XOO2II (+6 25$1*(
(D Anchor)
6L]H 3KRWR
*3
/HIW 3KRWR5LJKW 3KRWR*3/HIW 5LJKW
*X\3XOO2II
*X\3XOO2II
*X\3XOO2II
*X\3XOO2II
*X\3XOO2II
&DEOH6L]H
PHDVXUHPHQW
6HH1RWHDERYH
3DLQW
&RORURQ
'HDG(QG
*ULS,I
YLVLEOH
0HDVXUHG7HQVLRQ/EV
8VH*3/HIWFROXPQIRU
*X\3XOO2II
6HH1RWHDERYH
'HVLJQ
,QLWLDO
7HQVLRQ
RI%6
&DOFXODWHG7HQVLRQ
RI'HVLJQ
'HVLJQ
,QLWLDO
7HQVLRQ
RI%6
&DOFXODWHG7HQVLRQ
RI'HVLJQ
'LVW7R
$QFKRU
)W
*X\
$WWDFKPHQW
7\SH
&DEOH
7\SH
&DEOH6L]H
PHDVXUHPHQW
6HH1RWHDERYH
3DLQW
&RORURQ
'HDG(QG
*ULS,I
YLVLEOH
0HDVXUHG7HQVLRQ/EV
8VH*3/HIWFROXPQIRU
*X\3XOO2II
6HH1RWHDERYH
&RPPHQWV
&RPPHQWV
7HPS
)
7HPS
)
*X\
/HYHO (OHY)W
*X\
/HYHO (OHY)W
'LVW7R
$QFKRU
)W
*X\
$WWDFKPHQW
7\SH
&DEOH
7\SH
6LWH 6LWH1DPH &RQWUDFWRU1DPH &RPSOHWHG%\ 'DWH ):)W(OHY)WTower Plumb and Twist Measurements:LQG6SHHG 'LUHFWLRQ 66: 'DWD3RLQW0DVW(OHY
6HH1RWH)W$)DFH:LGWK,Q/HJ:LGWK,Q'
L ' L ' LG,QHD'HJ[,Q\,QU,Q * Mast Elevation Note** Displacement Note'UHIHUVWRGLUHFWLUHIHUVWRLQYHUVH8QLWOHVVYDOXHVDUHIUDFWLRQRIOHJGLVSODFHG)RUJX\HGWRZHUVUHFRUGGDWDDWHDFKJX\HOHYDWLRQandDWDOOWDSHUFKDQJHHOHYDWLRQV)RUVHOIVXSSRUWLQJWRZHUVUHFRUGGDWDDWHDFK
VHFWLRQandDWDOOWDSHUFKDQJHHOHYDWLRQV*For a GT w/ a tapered base, enter the face widthat the top of the taper into Cell H14.3267$'-8670(176,'('72:(57:,67$1'3/80%7KHWUDQVLWLVWREHVHWXSRQHDFKOHJD]LPXWKDWWKHEDVHRIWKHWRZHU7KHFRUUHVSRQGLQJWRZHUOHJDWWKHEDVHRIWKHWRZHULVXVHGWRVHWWKHYHUWLFDOEDVHOLQH2%6(59('/(*',63/$&(0(176&$/&8/$7('7:,67&$/&8/$7('2872)3/80%&RPPHQWVWK7DSHU&KDQJHOR7RSRI7RZHUUG7DSHU&KDQJHOR7RSRI7RZHUQG7DSHU&KDQJHOR7RSRI7RZHUVW7DSHU&KDQJHOR7RSRI7RZHU%DVHRIWRZHU%RWWRPRIVWHHO
86)/)35)06WXGLR:LOOLDP6KHSSDUG